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http://www.fortmcmurraytoday.com ... -and-pipeline-spill
/ c2 S- u+ l; JNexen Energy will lay off about 350 workers from its Long Lake facility, following its release of results of internal investigations into a July 2015 pipeline spill and the January 2016 hydrocracker explosion.# l' E% n! v% V7 Q8 Q$ v2 I
7 j# A4 w; l G1 Q) V$ cThe CNOOC-owned energy company will only be continuing its steam-assisted gravity drainage (SAGD) operations at Long Lake, after it determined a short-term repair was not possible for the hydrocracker unit, which killed two employees when it exploded on Jan. 15, 2016.6 f; j3 ?7 R- N" B$ L8 s H% b
9 I: Q. l% ]4 b6 c2 EThe facility's upgrader has been idling since then, and will be moved into winter preservation, with no estimation of when it will be brought back into service.' ^% b. ]4 c. S/ a( |) I
! o; b1 c7 H( z3 x8 BAn internal investigation found the explosion was a result of work being performed that was "outside of the scope of approved work activities.") e5 y" D& y3 Y( Q$ [8 [' c3 p: \
$ l& f+ c( A6 Y( ~The two employees killed, both Fort McMurray residents, were 52-year-old Drew Foster and 30-year-old Dave Williams. Foster was killed in the explosion. Williams, who was flown to the University of Alberta Hospital's burn unit hours after the explosion, died a week later.
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\ H3 j, [0 X) NIn its announcement Nexen said it is addressing safety gaps in part with refresher training on workplace hazard identification, increased site supervision and safety inspections. 1 \& m4 J4 d: c
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The decision to move to a SAGD-only operation was described as "entirely economic," and will result in about 350 staff layoffs, most of which will be completed by the end of 2016.
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; @) v% V+ M; p% l \The results of the investigations were given at a news conference on Tuesday by Nexen CEO Fang Zhi and Senior Vice President of Canadian Operation Ron Bailey.
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% X+ C( T/ Y9 \ A9 [* j+ YNexen also said it found the root cause of a July 2015 emulsion spill at Long Lake to be a "thermally-driven upheaval buckling of the pipeline, and the subsequent cooldown during the turnaround."
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This was caused because of pipeline design incompatible with the muskeg ground conditions, and steps that could have been taken to mitigate the potential for buckling were not addressed. , S; _$ _; H! p! x( y% O* b% I& B9 N
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The spill poured up to five million litres of emulsion - a mixture of water, bitumen and sand - into surrounding muskeg. The spill may have been ongoing for up to two weeks when it was discovered in July 2015 by a contractor walking through the area.
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In August the Alberta Energy Regulator ordered Nexen to shut down 95 pipelines until the company could prove the pipelines could be operated responsibly. The suspension was lifted in September 2015. 1 p; E5 ^. {4 c
. h) o z, c' \0 W1 C- with files from Vincent McDermott |
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