 鲜花( 10)  鸡蛋( 0)
|
http://www.fortmcmurraytoday.com ... -and-pipeline-spill
U$ W& \5 a& ^1 c' s5 }Nexen Energy will lay off about 350 workers from its Long Lake facility, following its release of results of internal investigations into a July 2015 pipeline spill and the January 2016 hydrocracker explosion.' g+ @. P; F: Z8 \, m
' m8 Q# j6 ?8 [9 QThe CNOOC-owned energy company will only be continuing its steam-assisted gravity drainage (SAGD) operations at Long Lake, after it determined a short-term repair was not possible for the hydrocracker unit, which killed two employees when it exploded on Jan. 15, 2016.. x' A* ?6 X0 `/ X" x
; o( Y2 f. ~+ ]1 z# s8 X2 M( n
The facility's upgrader has been idling since then, and will be moved into winter preservation, with no estimation of when it will be brought back into service.
% D$ `1 X; f# N4 {2 {+ M* U' E9 o
/ q) W* j/ ~/ Y+ O+ {" NAn internal investigation found the explosion was a result of work being performed that was "outside of the scope of approved work activities."; E8 B2 t- k1 {$ _
% v6 f' p9 G WThe two employees killed, both Fort McMurray residents, were 52-year-old Drew Foster and 30-year-old Dave Williams. Foster was killed in the explosion. Williams, who was flown to the University of Alberta Hospital's burn unit hours after the explosion, died a week later.
8 Z9 U( e+ v% S* s4 g* C3 `5 d. p0 G2 I6 F6 ^& I% E
In its announcement Nexen said it is addressing safety gaps in part with refresher training on workplace hazard identification, increased site supervision and safety inspections.
$ G9 v z9 L) f( r7 z' r
) j/ |# T# s7 d! C1 G* BThe decision to move to a SAGD-only operation was described as "entirely economic," and will result in about 350 staff layoffs, most of which will be completed by the end of 2016.
8 w% @( p5 _' F. |8 E$ }& k [& p6 x7 `1 n" @8 B
The results of the investigations were given at a news conference on Tuesday by Nexen CEO Fang Zhi and Senior Vice President of Canadian Operation Ron Bailey.
9 H- h: R5 `( i$ `4 [1 O `$ B4 |
Nexen also said it found the root cause of a July 2015 emulsion spill at Long Lake to be a "thermally-driven upheaval buckling of the pipeline, and the subsequent cooldown during the turnaround."% Q) U, d* V) H
8 r6 V" f d! g, G
This was caused because of pipeline design incompatible with the muskeg ground conditions, and steps that could have been taken to mitigate the potential for buckling were not addressed.
) D0 C* B a0 k& d+ l- o/ K+ G) X P
The spill poured up to five million litres of emulsion - a mixture of water, bitumen and sand - into surrounding muskeg. The spill may have been ongoing for up to two weeks when it was discovered in July 2015 by a contractor walking through the area. ! }7 v: k, [ c# c
* d* J& F0 O+ j [! k. Z+ T
In August the Alberta Energy Regulator ordered Nexen to shut down 95 pipelines until the company could prove the pipelines could be operated responsibly. The suspension was lifted in September 2015. * l1 G1 U. X4 w: h5 w7 }
; H6 q8 F" I' m8 \9 C$ O- with files from Vincent McDermott |
|