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http://www.fortmcmurraytoday.com ... -and-pipeline-spill
+ L, N8 K% e% w4 C D% ZNexen Energy will lay off about 350 workers from its Long Lake facility, following its release of results of internal investigations into a July 2015 pipeline spill and the January 2016 hydrocracker explosion.' S6 f, I/ {" X- a
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The CNOOC-owned energy company will only be continuing its steam-assisted gravity drainage (SAGD) operations at Long Lake, after it determined a short-term repair was not possible for the hydrocracker unit, which killed two employees when it exploded on Jan. 15, 2016.
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' D7 E+ f2 j% RThe facility's upgrader has been idling since then, and will be moved into winter preservation, with no estimation of when it will be brought back into service.
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& n) T# ^" F: a8 z0 lAn internal investigation found the explosion was a result of work being performed that was "outside of the scope of approved work activities."4 a( n* o& q3 T: G
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The two employees killed, both Fort McMurray residents, were 52-year-old Drew Foster and 30-year-old Dave Williams. Foster was killed in the explosion. Williams, who was flown to the University of Alberta Hospital's burn unit hours after the explosion, died a week later.
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. V' e" @1 a2 X$ O- J0 aIn its announcement Nexen said it is addressing safety gaps in part with refresher training on workplace hazard identification, increased site supervision and safety inspections.
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The decision to move to a SAGD-only operation was described as "entirely economic," and will result in about 350 staff layoffs, most of which will be completed by the end of 2016. + t( I/ P7 c$ f7 h% z7 k7 d% Q
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The results of the investigations were given at a news conference on Tuesday by Nexen CEO Fang Zhi and Senior Vice President of Canadian Operation Ron Bailey./ ?. Q6 l1 x6 P
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Nexen also said it found the root cause of a July 2015 emulsion spill at Long Lake to be a "thermally-driven upheaval buckling of the pipeline, and the subsequent cooldown during the turnaround."
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This was caused because of pipeline design incompatible with the muskeg ground conditions, and steps that could have been taken to mitigate the potential for buckling were not addressed.
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/ X8 p. l4 }3 p3 @' tThe spill poured up to five million litres of emulsion - a mixture of water, bitumen and sand - into surrounding muskeg. The spill may have been ongoing for up to two weeks when it was discovered in July 2015 by a contractor walking through the area. / ?- [1 _* v+ J9 q0 q
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In August the Alberta Energy Regulator ordered Nexen to shut down 95 pipelines until the company could prove the pipelines could be operated responsibly. The suspension was lifted in September 2015.
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. J% I$ m) r0 z" ]! D; N# v1 k- with files from Vincent McDermott |
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