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http://www.fortmcmurraytoday.com ... -and-pipeline-spill
( d/ s8 s q! [% @/ Z9 i' dNexen Energy will lay off about 350 workers from its Long Lake facility, following its release of results of internal investigations into a July 2015 pipeline spill and the January 2016 hydrocracker explosion.
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6 X* ]% W, V8 v4 HThe CNOOC-owned energy company will only be continuing its steam-assisted gravity drainage (SAGD) operations at Long Lake, after it determined a short-term repair was not possible for the hydrocracker unit, which killed two employees when it exploded on Jan. 15, 2016.
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- l8 y5 f) ?: P! i* ]The facility's upgrader has been idling since then, and will be moved into winter preservation, with no estimation of when it will be brought back into service.
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An internal investigation found the explosion was a result of work being performed that was "outside of the scope of approved work activities."
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The two employees killed, both Fort McMurray residents, were 52-year-old Drew Foster and 30-year-old Dave Williams. Foster was killed in the explosion. Williams, who was flown to the University of Alberta Hospital's burn unit hours after the explosion, died a week later. . l; y8 K% }( I9 D0 L* |
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In its announcement Nexen said it is addressing safety gaps in part with refresher training on workplace hazard identification, increased site supervision and safety inspections.
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2 s3 i' |/ v1 u9 i9 g, [8 NThe decision to move to a SAGD-only operation was described as "entirely economic," and will result in about 350 staff layoffs, most of which will be completed by the end of 2016. ' C+ x. ^% S' y3 a( X0 Y! z
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The results of the investigations were given at a news conference on Tuesday by Nexen CEO Fang Zhi and Senior Vice President of Canadian Operation Ron Bailey.
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: ~, T8 [9 Q) W$ s: ]Nexen also said it found the root cause of a July 2015 emulsion spill at Long Lake to be a "thermally-driven upheaval buckling of the pipeline, and the subsequent cooldown during the turnaround."0 j- B# t, P/ `. k# ^
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This was caused because of pipeline design incompatible with the muskeg ground conditions, and steps that could have been taken to mitigate the potential for buckling were not addressed. . a4 H/ H- E0 A( h
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The spill poured up to five million litres of emulsion - a mixture of water, bitumen and sand - into surrounding muskeg. The spill may have been ongoing for up to two weeks when it was discovered in July 2015 by a contractor walking through the area. 6 c; p5 W4 s4 n7 c8 W0 n
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In August the Alberta Energy Regulator ordered Nexen to shut down 95 pipelines until the company could prove the pipelines could be operated responsibly. The suspension was lifted in September 2015. " [2 m/ I, c0 E8 H1 N
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- with files from Vincent McDermott |
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