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http://www.fortmcmurraytoday.com ... -and-pipeline-spill+ l2 X$ @/ y% Q$ J, i" _* y
Nexen Energy will lay off about 350 workers from its Long Lake facility, following its release of results of internal investigations into a July 2015 pipeline spill and the January 2016 hydrocracker explosion.
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The CNOOC-owned energy company will only be continuing its steam-assisted gravity drainage (SAGD) operations at Long Lake, after it determined a short-term repair was not possible for the hydrocracker unit, which killed two employees when it exploded on Jan. 15, 2016.
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The facility's upgrader has been idling since then, and will be moved into winter preservation, with no estimation of when it will be brought back into service.6 X) v. q! \* V& f& o I
9 p7 Y+ x4 e# A4 l5 y8 D$ O$ mAn internal investigation found the explosion was a result of work being performed that was "outside of the scope of approved work activities."
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+ J9 F+ O! ]& _3 s1 }( E& ~; b' zThe two employees killed, both Fort McMurray residents, were 52-year-old Drew Foster and 30-year-old Dave Williams. Foster was killed in the explosion. Williams, who was flown to the University of Alberta Hospital's burn unit hours after the explosion, died a week later. 3 | S2 ?0 e3 T9 m+ Q
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In its announcement Nexen said it is addressing safety gaps in part with refresher training on workplace hazard identification, increased site supervision and safety inspections. * G& o3 ^7 m7 o: @
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The decision to move to a SAGD-only operation was described as "entirely economic," and will result in about 350 staff layoffs, most of which will be completed by the end of 2016.
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The results of the investigations were given at a news conference on Tuesday by Nexen CEO Fang Zhi and Senior Vice President of Canadian Operation Ron Bailey. F* ~( [/ Y: U; S) g7 Z y
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Nexen also said it found the root cause of a July 2015 emulsion spill at Long Lake to be a "thermally-driven upheaval buckling of the pipeline, and the subsequent cooldown during the turnaround."
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This was caused because of pipeline design incompatible with the muskeg ground conditions, and steps that could have been taken to mitigate the potential for buckling were not addressed.
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2 t/ A. t" F1 ~8 B2 z. XThe spill poured up to five million litres of emulsion - a mixture of water, bitumen and sand - into surrounding muskeg. The spill may have been ongoing for up to two weeks when it was discovered in July 2015 by a contractor walking through the area.
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In August the Alberta Energy Regulator ordered Nexen to shut down 95 pipelines until the company could prove the pipelines could be operated responsibly. The suspension was lifted in September 2015. / R) ` z f% Q7 j' x8 d. a! b
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- with files from Vincent McDermott |
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