 鲜花( 10)  鸡蛋( 0)
|
http://www.fortmcmurraytoday.com ... -and-pipeline-spill
) F- }) _1 V8 a& ?0 ^Nexen Energy will lay off about 350 workers from its Long Lake facility, following its release of results of internal investigations into a July 2015 pipeline spill and the January 2016 hydrocracker explosion.2 L8 n' x# U% d
$ ~* q9 L: ~" D2 z+ zThe CNOOC-owned energy company will only be continuing its steam-assisted gravity drainage (SAGD) operations at Long Lake, after it determined a short-term repair was not possible for the hydrocracker unit, which killed two employees when it exploded on Jan. 15, 2016., i. k: H) R4 h2 M7 b: W2 X B
. c& {4 [% y2 @$ n
The facility's upgrader has been idling since then, and will be moved into winter preservation, with no estimation of when it will be brought back into service.5 `. y2 Y4 f; g6 @. G
) X9 J }9 ?9 }1 J( P6 xAn internal investigation found the explosion was a result of work being performed that was "outside of the scope of approved work activities."
. l" l) s# B8 o/ {5 W( L6 s4 S7 V3 V: ?
The two employees killed, both Fort McMurray residents, were 52-year-old Drew Foster and 30-year-old Dave Williams. Foster was killed in the explosion. Williams, who was flown to the University of Alberta Hospital's burn unit hours after the explosion, died a week later. ) W6 O- l( [6 k4 P! R$ w
2 e% E2 }( ]' A# C B. P
In its announcement Nexen said it is addressing safety gaps in part with refresher training on workplace hazard identification, increased site supervision and safety inspections. ~( F$ B# ?: x: i K
$ P b1 e* D( {; {The decision to move to a SAGD-only operation was described as "entirely economic," and will result in about 350 staff layoffs, most of which will be completed by the end of 2016. % M5 p4 r, O) x! \, T" h
$ I9 X( ~ j6 _4 a1 l
The results of the investigations were given at a news conference on Tuesday by Nexen CEO Fang Zhi and Senior Vice President of Canadian Operation Ron Bailey.
& e( F- w' B: ?0 D% w( [. w$ A3 z1 U+ a
Nexen also said it found the root cause of a July 2015 emulsion spill at Long Lake to be a "thermally-driven upheaval buckling of the pipeline, and the subsequent cooldown during the turnaround."! u3 Q' V( H7 S1 l! C* i
$ ]2 g. j+ i' P f H0 s9 l9 `: }
This was caused because of pipeline design incompatible with the muskeg ground conditions, and steps that could have been taken to mitigate the potential for buckling were not addressed.
0 M$ _2 G) J5 k$ S+ S; D* O; o; d( h" o2 r" i4 L: ?6 f
The spill poured up to five million litres of emulsion - a mixture of water, bitumen and sand - into surrounding muskeg. The spill may have been ongoing for up to two weeks when it was discovered in July 2015 by a contractor walking through the area. : d% F5 `. l$ l7 L8 o8 M, N2 a6 d
5 \7 `0 e/ M, Y6 Q2 b: {In August the Alberta Energy Regulator ordered Nexen to shut down 95 pipelines until the company could prove the pipelines could be operated responsibly. The suspension was lifted in September 2015.
2 j4 J# p1 ]. _2 M6 y- m
P7 B) l- @3 a6 x3 V- with files from Vincent McDermott |
|