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http://www.fortmcmurraytoday.com ... -and-pipeline-spill
3 w6 w) R( V7 L k; J1 dNexen Energy will lay off about 350 workers from its Long Lake facility, following its release of results of internal investigations into a July 2015 pipeline spill and the January 2016 hydrocracker explosion.5 ^6 `0 ~1 Y5 v6 R5 Z& h
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The CNOOC-owned energy company will only be continuing its steam-assisted gravity drainage (SAGD) operations at Long Lake, after it determined a short-term repair was not possible for the hydrocracker unit, which killed two employees when it exploded on Jan. 15, 2016.
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! u$ M" N4 r, {) x4 cThe facility's upgrader has been idling since then, and will be moved into winter preservation, with no estimation of when it will be brought back into service.
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An internal investigation found the explosion was a result of work being performed that was "outside of the scope of approved work activities."9 W) A9 |- H' l0 _1 x4 |1 ~
# V, u+ B5 u, ]! [The two employees killed, both Fort McMurray residents, were 52-year-old Drew Foster and 30-year-old Dave Williams. Foster was killed in the explosion. Williams, who was flown to the University of Alberta Hospital's burn unit hours after the explosion, died a week later. 4 L0 c9 c8 h) B% z
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In its announcement Nexen said it is addressing safety gaps in part with refresher training on workplace hazard identification, increased site supervision and safety inspections.
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* P# H& L# Z9 B1 FThe decision to move to a SAGD-only operation was described as "entirely economic," and will result in about 350 staff layoffs, most of which will be completed by the end of 2016. 1 Y: V# q3 i" b S
* i7 q0 z) F$ K7 I) iThe results of the investigations were given at a news conference on Tuesday by Nexen CEO Fang Zhi and Senior Vice President of Canadian Operation Ron Bailey.
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Nexen also said it found the root cause of a July 2015 emulsion spill at Long Lake to be a "thermally-driven upheaval buckling of the pipeline, and the subsequent cooldown during the turnaround."0 ~( K5 @# k, C& B1 T& [
6 q# M, ]9 o- q, _9 J7 q5 i/ T4 ZThis was caused because of pipeline design incompatible with the muskeg ground conditions, and steps that could have been taken to mitigate the potential for buckling were not addressed.
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The spill poured up to five million litres of emulsion - a mixture of water, bitumen and sand - into surrounding muskeg. The spill may have been ongoing for up to two weeks when it was discovered in July 2015 by a contractor walking through the area.
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In August the Alberta Energy Regulator ordered Nexen to shut down 95 pipelines until the company could prove the pipelines could be operated responsibly. The suspension was lifted in September 2015. / F: X% \* w/ M3 P$ R2 c: ]
1 F' I0 p+ B* V) V- with files from Vincent McDermott |
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